Same here. Just updated to 10714 and the forces are much stronger.
Small MiGe Biss-C. Tested with iracing. Also had to reduce Damping, Friction and Inertia by a big margin.Small MiGE Biss-C 4.2milcpr.drc (9.4 KB)
Thanks all, we will look into this. It didnāt affect my setup at home, but I do not have a realistic steering wheel attached to my small Mige. In fact, it is a piece of cardboard at the momentā¦
Less oscillations more smoothly sound goodā¦
Hi,
After the update I got an Error ID1: 610 so I have changed my MMC value from 24.5A to 18A and then I had another Error ID1: 440501 so I changed FOV from 51 DC Volts to 50 and FUV on 25 DC Volts and now it works again.
So far I can say the maximum MMC on this ioni 1.7.14 is 18A. I canāt go any more than 18A maybe Iām doing something wrong.
My Spec:
Large mige biss-c 0.50.4 and ioni 1.7.14
Simucube hardware version: Revision 2 (r005)
This is DRC im using right now.
[X] Initialized
[ ] Error recovering
[ ] Tracking error warn
[ ] Target reached
[X] Enabled
[X] Run (drive active)
[ ] Homing active
[ ] Braking
[ ] Permanent stop
[X] Voltages good
[ ] Fault stopped
[X] Ready for use
[ ] STO active
[ ] Safe torque mode
[X] Standing still
[ ] Quick stop active
[ ] Tracking error
[ ] Over velocity
[ ] Hardware
[ ] Over temperature
[ ] Feedback
[ ] Over current
[ ] Internal comm error
[ ] Power stage forced off
[ ] Under voltage
[ ] Over voltage
[ ] Motion range
[ ] Firmware error
[ ] Init
[ ] Motion
[ ] SimpleMotion
[ ] Configuration
Fault location ID1 0 (info)
Fault location ID2 0 (info)[X] GPI 1
[X] GPI 2
[ ] GPI 3
[ ] GPI 4
[X] GPI 5
[ ] GPI 6
[ ] HSIN 1
[ ] HSIN 2
[ ] ANA1 as digital
[ ] ANA2 as digital
[X] ENC A
[X] ENC B
[X] ENC C
[ ] ENC D
[X] Hall U
[X] Hall V
[X] Hall W
[X] Soft enable
[X] Phys enable
[ ] Pos feed enable
[X] Neg feed enable
[X] Home switch
[ ] Clear faults
Analog in 1 1.34 V
Analog in 2 0.00 V
Analog Enc A 1.23 V
Analog Enc B 1.24 V
HV bus voltage 48.0 VDC
Device temperature 27 Ā°C
Actual current limit Ā±24.5 A
Last limit reason None
Output current 0.01 A
Velocity feedback -0.00119 r/s
Velocity feedback (raw) -2
Position feedback -0.000140429 r
Position feedback (raw) -589
Setpoint value (raw) 0
Debug 1 -1
Debug 2 -1
Debug 3 -1
Debug 4 -1
Debug 5 -1
Debug 6 -1
Parameters
| GCFWVER=10710 | HWTYPE=11201 | HWSERIAL=112012576 | BUILDREVISION=7989452
| CEI=2 | UID=77710a2 | SMO=0 | TRF1=0
| TRF2=0 | TRA1=0 | TRA2=0 | MPP=720
| NOTCHFILT=655616 | TED=2 | TEF=0.5 | TEI=0
| SERIALENCBITS=22 | COMMUTATIONCFG=0 | HAO=0 | FBR=1.04858e+06
| FBD=5 | FB2D=0 | TBW=11 | KVP=0
| KVI=0 | KPP=0 | VFF=0 | AFF=0
| PFF=0 | CM=2 | MT=3 | AD=0
| FLAGS=131100 | MMC=24.5 | MCC=13.25 | FOC=6
| FOV=51 | FUV=25 | FPT=0 | FVT=0
| FEV=11000 | FMO=0 | LSF=0 | LFO=0
| AXS=1 | AXT=3 | FFT=0 | TSR=0
| TCH=0 | TTR=1 | TBT=0 | CRI=3
| DIV=100 | PIF=2500 | MUL=100 | CAL=10
| CSD=10 | CVL=1000 | CRV=0 | MR=1.23
| ML=4.451 | MTC=2360 | MPC=8 | MMS=1500
| CAO=0 | HOMING=0 | HMV=100 | HMA=10
| HMH=0 | HMT=1 | HHL=0 | HLL=0
| HMF=0 | HSA=0 | HSS=0 | overrideAddr1=0
| overrideAddr2=0 | overrideAddr3=0 | overrideVal1=0 | overrideVal2=0
| overrideVal3=0 | BED=1.5 | BER=0 | BDD=1
| CAPS1=6.29143e+07 | CAPS2=81823
Thanks for the detailed report.
It seems that the IONI works at the end, but it would be a support nightmare if popular setups would need to get reconfigured in order to work with this firmware. So, no official Simucube test build yet until we solve this.
Large mige biss-c 0.50.4 and ioni 1.7.14
Simucube hardware version: Revision 2 (r005)
Quick update, after the update to ioni 1.7.14 Iāve dropped down the MMC from 24.5A to 14A and MCC from 18A to 12A everything is working, only x2 stronger. I had a few laps in different games and everything seems to be much stronger even after dropping down MMC, MCC and yes it feels a bit smoother and more responsive.
Thanks for continuing the support for SC1 I appreciate this so much!
Hi @JerryS,
We have identified the issue with the 1.7.14 version; it relates to particular IONI versions (Pro HC).
We would advice you to downgrade and NOT USE 1.7.14 at this point.
We have removed IONI firmware version 1.7.14 from download page.
@JerryS has been given Accomplished Bug Hunter badge due to his great, comprehensive debug data. Must have been fastest ever from the time of joining! Welcome to the forum.
Congratulations, JerryS
We have a closed beta shortly for IONI issue. Is @Herve45 or any others interested to test that?
Yes
I am ready to test tomorrow
I am available to test
I could test too if you want.
Did any of you try the 1.7.14 and had the stronger forces -issue?
Yes I tried the 1.7.14 and had the stronger forces -issue
Small mige
Biss-c
Ioni pro hc
Simucube 0.50.4
Beta has been shared to few of the above posters.
Promisingly good news from the beta testers.
There has been another round of important developments being done for the Simucube 2 firmware, and likely we will finish some of those, import to Simucube 1, and then test release.
Beta testers on iRacing please try something for me.
Stop on the track and do some spins (doughnuts) in both directions.
Please be careful just in case there is a bug that we just found in an earlier Simucube firmware which causes the wheel to just take off spinning.
If you have the IR18 Indycar please do the test in that car also.
Thanks,
Joe
Irrelevant, the beta was just IONI firmware which does not handle any bumpstop stuff.