[ ] Initialized ! [ ] Error recovering [ ] Tracking error warn [ ] Target reached [X] Enabled [ ] Run (drive active) [ ] Homing active [ ] Braking [X] Permanent stop ! [X] Voltages good [X] Fault stopped ! [ ] Ready for use [ ] STO active [ ] Safe torque mode [ ] Standing still [ ] Quick stop active [ ] Tracking error [ ] Over velocity [ ] Hardware [ ] Over temperature [ ] Feedback [ ] Over current [ ] Internal comm error [ ] Power stage forced off [X] Under voltage ! [ ] Over voltage [ ] Motion range [ ] Firmware error [X] Init ! [ ] Motion [ ] SimpleMotion [ ] Configuration What caused this fault? Fault location ID1 440502 (info) Fault location ID2 0 (info) ! = reasons for inactivity[X] GPI 1 [X] GPI 2 [X] GPI 3 [ ] GPI 4 [X] GPI 5 [ ] GPI 6 [ ] HSIN 1 [ ] HSIN 2 [ ] ANA1 as digital [ ] ANA2 as digital [ ] ENC A [ ] ENC B [ ] ENC C [ ] ENC D [ ] Hall U [X] Hall V [X] Hall W [X] Soft enable [X] Phys enable [ ] Pos feed enable [ ] Neg feed enable [X] Home switch [ ] Clear faults Analog in 1 1.49 V Analog in 2 0.00 V Analog Enc A -3.45 V Analog Enc B -3.44 V HV bus voltage 47.9 VDC Device temperature 32 °C Actual current limit ±12.9 A Last limit reason Voltage limit Output current 0.00 A Velocity feedback 0 r/s Velocity feedback (raw) 0 Position feedback -0.001275 r Position feedback (raw) -51 Setpoint value (raw) 0 Debug 1 -1 Debug 2 -1 Debug 3 -1 Debug 4 -1 Debug 5 -1 Debug 6 -1 Parameters | GCFWVER=10714 | HWTYPE=11201 | HWSERIAL=112013267 | BUILDREVISION=182510c5 | CEI=2 | UID=356c814a | SMO=0 | TRF1=0 | TRF2=0 | TRA1=0 | TRA2=0 | MPP=960 | NOTCHFILT=655616 | TED=0 | TEF=0.5 | TEI=0.5 | SERIALENCBITS=6 | COMMUTATIONCFG=0 | HAO=0 | FBR=10000 | FBD=1 | FB2D=0 | TBW=11 | KVP=2200 | KVI=30 | KPP=50 | VFF=0 | AFF=0 | PFF=85 | CM=2 | MT=3 | AD=0 | FLAGS=131092 | MMC=12.86 | MCC=10.5 | FOC=4 | FOV=49.5 | FUV=30 | FPT=1000 | FVT=100 | FEV=140 | FMO=0 | LSF=0 | LFO=0 | AXS=1 | AXT=3 | FFT=0.1 | TSR=15 | TCH=126 | TTR=1 | TBT=0 | CRI=3 | DIV=50 | PIF=2500 | MUL=50 | CAL=32 | CSD=10 | CVL=1400 | CRV=100 | MR=2.905 | ML=8.723 | MTC=3260 | MPC=8 | MMS=1000 | CAO=0 | HOMING=0 | HMV=100 | HMA=10 | HMH=500 | HMT=1 | HHL=0 | HLL=0 | HMF=0 | HSA=0 | HSS=0 | overrideAddr1=0 | overrideAddr2=0 | overrideAddr3=0 | overrideVal1=0 | overrideVal2=0 | overrideVal3=0 | BED=1.5 | BER=0 | BDD=1 | CAPS1=6.29143e+07 | CAPS2=81823