Communication fault location id: 480701

Don’t know if this is something i should be worried about ("Motor faults: Communication fault Fault location ID: 480701)

Started iracing and no FFB.
Shut down and power on again fixed the issue

Below the debug log:
Timestamp : 2051

Wireless: State change : 2

Simucube Boot : 1

Simucube Boot : 0

Simucube Boot : 10

Flash settings data loaded : 0

First-time drive initialization : 0

Initial config has been previously performed. Initializing Drive. : 0

State: Initializing Drive : 0

Drive Firmware update : 0

Drive firmware updated successfully : 0

Command: Request profile number : 0

Command: Request profile name for profile : 0

Command: Request profile byte data for profile : 0

Command: Request profile number : 1

Command: Request profile name for profile : 1

Command: Request profile byte data for profile : 1

Command: Request profile number : 2

Command: Request profile name for profile : 2

Command: Request profile byte data for profile : 2

Command: Request profile number : 3

Command: Request profile name for profile : 3

Command: Request profile byte data for profile : 3

Timestamp : 3807

Wireless: State change : 3

Command: Request hardware settings : 0

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 0

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 1

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 2

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 3

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 4

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 5

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 6

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 7

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 8

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 9

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 10

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 11

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 12

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 13

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 14

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 15

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 16

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 17

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 18

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 19

Command: Request analog input settings : 0

Command: Request bytedata for analog profile : 20

Command: Set calibrated analog axis mode : 0

Drive init stage 1, position : 1238204

Read MMC value from Drive : 22800

Read Motor Resistance value from Drive : 700

Read CPR from Drive : 4194304

Read Drive Version ID from drive : 40000

Simucube 2 Serial Number : 762

SM Watchdog disabled successfully : 0

Successfully applied DRC data to Drive : 0

Read MMC value from Drive : 22800

Read Motor Resistance value from Drive : 700

Read CPR from Drive : 4194304

Read Drive Version ID from drive : 40000

Simucube 2 Serial Number : 762

Waiting for servo to be ready : 0

Drive init stage 3, position after faults cleared : 1238204

Drive init stage 4, phasing, current position : 1238204

Drive init stage 4, phasing, current position : 1238204

Drive init stage 4, phasing, current position : 1238204

Drive init stage 4, phasing, current position : 1238216

State: Drive initialization was successful : 0

State: Set baudrate : 0

SM Watchdog enabled successfully : 0

SMBus baudrate initialized successfully : 4500000

State: Before operational - calculating new constant values : 0

State: Operational : 0

Command: Event log download request : 0

Command: Start event logging : 0

event 260 : 0

event 261 : 0

event 262 : 0

Command: Event log download request : 0

Toggling the e-stop also clears the faults. We are investigating this and few other communication faults that some people seem to be getting. However, we do not have reports that faults happen while driving.

ok thanks for your reply

I have a feeling this happens while having e-stop pushed, then turning on the SC2 power, and then starting the Truedrive software.

Currently I am always releasing the e-stop berfore turning on the power because of this.

Though reseting the ”failure” as according to Mika works.